The coach on the lifting jacks, minus its bogies.
The south end bogie has been rolled clear, the problem axle was on the north end bogie, inner axle.
The brake linkage on the problem bogie is being removed. Richard (nearest camera) with Bill wielding the spanners.
Bennie removing the dynamo belt.
With assistance from Ralph and Jack.
The bogie under the lifting gantry, this end has been lifted and the axle rolled out.
The replacement axle being prepared, prior to fitting. Both axles were changed to keep the wheel diameters within 1.5mm of each other. This is a requirement because of non compensating brakes, if the wheel diameters were very different, the brakes on one axle wouldn't reach the wheel.
Also whilst this was going on, all brake blocks were renewed, as well as the dust shields on the replacement axles.
The bogie back in place with its replacement axles, so far so good!
One of the consequences of having to put another coach on the jacks is a mega shunt.
Mark 2 BFK 17101
Some progress, mainly on replacing the floors in the two remaining compartments.
The end capping, prior to fitting the corridor connection bellows.
A compartment floor, bottom ply is down and covered with the expanded foam sheet.
More compartment views
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